The Mean Green Stingray
Gets a new 427
Come back soon to see the install of this little beast in Travis' '69 coupe.
May 5: Wow, lots of problems for the 'lil 427.  We got the motor done and installed and made a glorious 7 minute run.  Started up great, sounded insane coming straight out of the headers, but it died after 7 minutes.  I think it was just some trash in the carburetor but it was a bit of a blessing in disguise.  Took the valve covers off to see how things looked and re-tq the head bolts and BAM, stripped out ALL of the upper bolt threads.  So the engine had to come back out for repairs.  Jim came over to help heli-coil the damaged threads and we had lots of troubles.  When we fixed the problem threads and tried bolting up the heads again a bunch more stripped out.  I ended up driving all over town buying up all the 7/16"-14 heli-coils I could find and we re-threaded ALL of the head threads in the block.
You think that's the end of it, right?  WRONG!  After all this work we decided using the old bolts was not a wise idea so I ordered some ARP head studs.  MORE problems.  Apparently we didn't tap the holes straight enough and when we put in the studs it looked like a porcupine.  We tried slipping the heads down on them but they were too misaligned.  Ended up having to take the bad ones out and bend over the rest with a 5' x 1" thick solid steel pry bar.  Wow, that was a little scary!
Well we finally got the heads on and the motor back in the vette in less than a week.

A HUGE thanks to Joe B, Rob N, Jim M, Tony A, and my Dad.
First Page
Original car
Painting block
Assembly Pg 1
Install Pg 1
Install Pg 2
Exhaust